SALEM - MANUAL REACTOR TRIP DUE TO LOSS OF CIRCULATORS AFTER UPTAKE OF RIVER ICE - NRC Event Reports
"A manual trip of Salem Unit 2 was initiated due to a loss of 4
circulators due to an excessive uptake of river ice. Strong northwest
winds, freezing temperatures and abnormally low tide levels contributed
to the ice formation on the river. The operating crew entered
EOP-TRIP-A, appropriately transitioned to EOP-TRIP-2 and stabilized the
plant at no load conditions (MODE 3 Hot Stand-by).
"All rods fully inserted on the trip and all systems responded as
designed with decay heat being removed via the Steam Dump system, with
condenser vacuum maintained. All three AFW Pumps auto started due to
low Steam Generator level due to closure of 21-23CN27, low pressure
feed water heater inlet isolation valves. There were no other
significant equipment challenges associated with the reactor trip.
"Salem Unit-2 is currently in mode 3. The Reactor Coolant System
temperature is 547 [degrees] F with pressure at 2235 psig [NOT and
NOP]. All ECCS and ESF Systems are available and no ECCS systems
actuated during the event. No personnel injuries occurred as a result
of the trip. [The Unit 2 reactor trip recovery is uncomplicated.]."
Unit 1 power was also reduced to 80%. Although the combination of
strong northwest winds, freezing temperatures and an abnormally low
tide contributed to the ice formation on the river, operators foresee
no further complication due to the ice conditions.
DUANE ARNOLD - DIESEL GENERATOR AUTO START DUE TO FAILED LINE ARRESTOR IN SWITCHYARD
"This report is being made under 10CFR50.72(b)(3)(iv)(A), 'Any
event or condition that results in valid actuation of any of the
systems listed in Paragraph (b)(3)(iv)(B) of this section' due to an
auto start of the 'A' Standby Diesel Generator.
"The auto start of the 'A' Standby Diesel Generator occurred on a
valid bus undervoltage condition caused by a momentary fault on the 161
kV Vinton line. Switchyard inspection revealed a failed 161 kV line
arrestor [on] one of the phases of the Vinton line. The 'A' Standby
Diesel Generator supply breaker was not required to close onto its
respective essential bus as it remained powered from its normal power
supply, 1X003 Start-up Transformer, during and after the event. Offsite
power remained fully operable during and following the event. The 'A'
Standby Diesel Generator has been returned to the standby/readiness
condition.
"As designed, the 'A' Emergency Service Water systems auto started
when the 'A' Standby Diesel Generator started. The Emergency Service
Water systems have been returned to the standby/readiness condition.
"The 'B' Well Water Pump tripped as a result of the electrical
transient. The 'A' Well Water pump and 'B' Emergency Service Water pump
were manually started by operators in accordance with Abnormal
Operating Procedure 408, Well Water System Abnormal Operation.
"The in-service Reactor Water Cleanup pump tripped which removed
RWCU from service. The RWCU system has been returned to service.
"The in-service Spent Fuel Pool Cooling pump tripped as a result of
the electrical transient. Spent Fuel Pool Cooling has been returned to
service. Spent fuel pool temperature rose 0.7 [degrees] F while the
pump was out of service.
"All ECCS systems were available before the event and have remained available following the event."
The licensee is not in any Technical Specification LCO's as a
result of this event. The in-service Spent Fuel Pool Cooling pump was
OOS for approximately 58 minutes.


